As soon as I get my head pipe off I'm going to do a leak down test. The motor ripped when I rode it with the 38mm TMX carb. All that I changed was putting the air striker on which started this entire reason for what I'm currently doing. After I put the carb on it wouldn't start so I took it off and cleaned it and thought while I have it that far apart I would do the compression test and other checks. It is a brand new piston and 72.25 bore, all new bearings and seals in the motor, new stock stroke new style Hot Rods crank, new Boyesen rad valve, new spark plug, and new race gas dome with fresh Sunoco 110. It definitely has more than 150psi compression because it kicks over harder than my Blaster that had a Baldwin ported national motor on the same fuel with a 34mm carb and over 150 psi compression. When I took the air striker carb apart it had a 52 pilot and 170 main but to me that doesn't matter at this point because it should still fire up so it may be an electrical issue as well. I'm confused but will head out to the garage tomorrow and see what I can find out.
udontknowme- I agree with you some what but to me with only 3-4 hours on a fresh motor it should definitely be over 155psi no matter what so I'm glad I decided to check it when I did. Hopefully it's just bad compression gauges. Would there be anything besides a air leak that would affect the compression that much?