pulling my hair out trying to figure out what is going on here. Have an 88 250r , started out as a stock motor, cylinder, first ride burned a hole in the top of the piston within ten minutes. Tore it completly down different set of cases, new bearings, new seals, LED ported and o-ringed the head. New V-force reeds new UPP intake, 38mm PWK 50 pilot, 180 main, DDJ 3rd clip, AV gas 32:1 w/HP2. Second trip same results ten min ride not even full throttle burned a quarter size hole in the top of the piston. Thought maybe not pulling enough fuel changed the petcock setup to the Honda CRF250x did the petcock mod to pull from both on and reserve, new piston ran 110 race fuel thinking the AV gas was the problem nope!! another less than ten minute ride 1/2 to 3/4 throttle at most torched the piston. Air leak ?? Going to try a leak down test not sure if the hole in the piston will effect the results but i don't know what else it could be even though it has all new seals. Any insight would be greatly appreciated.